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Steady state and transient measurements within a compressor rotor during steam-induced stall at transonic operational speeds

Approved for public release, distribution unlimited / Steam leakage from an aircraft carrier catapult is sometimes ingested into the aircraft engines upon launch which may induce compressor stall. Investigation of this phenomenon is of particular interest to the Navy with its new F35C, the aircraft carrier variant of the joint strike fighter. The single engine configuration of the F-35C makes this aircraft particularly vunerable to steam-induced stall. The present study examined both throttle-induced stall and steam-induced stall in a compressor at 90% and 95% speed through the use of 9 Kulite and 2 hot-film pressure transducers. The use of Fast Fourier Transform waterfall plots of the transient data before and during stall proved invaluable in determining stall precursors as well as the mode of rotor stall. In addition, a new computational fluid dynamic model was designed using CFX-5 software to represent a single blade passage of the compressor rotor, in order to predict compressor performance. The computed results were compared to experimental results gathered at various throttle settings. An accurate model will enable researchers to predict compressor performance for various and multiple gases. / Outstanding Thesis

Identiferoai:union.ndltd.org:nps.edu/oai:calhoun.nps.edu:10945/2528
Date09 1900
CreatorsZarro, Sarah E.
ContributorsHobson, Garth V., Shreeve, Raymond P., Naval Postgraduate School (U.S.), Department of Mechanical and Astronautical Engineering
PublisherMonterey, California. Naval Postgraduate School
Source SetsNaval Postgraduate School
Detected LanguageEnglish
TypeThesis
Formatxiv, 69 p. : ill. ;, application/pdf
RightsThis publication is a work of the U.S. Government as defined in Title 17, United States Code, Section 101. As such, it is in the public domain, and under the provisions of Title 17, United States Code, Section 105, may not be copyrighted.

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