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Chemical scrubbing of odorous gas generated from hot-melted coal

This study armed to develop a chemical scrubbing process to eliminate odorous VOCs (volatile organic compounds) in gases emitted from hot-melted coal tar used in bamboo antiseptic processing. Major VOCs are mono-aromatic hydrocarbons (MAHs), polycyclic aromatic hydrocarbons (PAHs), phenol and ammonia.
A pilot scrubber with a recycling scrubbing liquid tank and with an acrylic column of 0.10 m in length, 0.10 m in width, and 0.58 m in height, packed with 1¡¦¡¦ diameter plastic packings to a height of 0.38 m will be used for the scrubbing test of the emitted gas. Aqueous solutions of sodium hypochlorite (NaOCl), hydrogen peroxide (H2O2), detergent, and the Fenton¡¦s reagent (hydrogen peroxide with ferrous chloride) will be used as oxidants for the VOCs.
Results indicated that with operation conditions of VOCs 20-30 ppm (as methane), an empty bed retention time (EBRT) of around 28.5 s in the packed section, and a sodium hypochlorite concentration of 450 mg Cl2/L with pH of 6, around 45.3-50.3% of the VOCs in the influent gas could be removed at a L/G (liquid to gas flow rate ratio) of 0.295 m3/m3. A test indicated that the overall odor(expressed as the dilution to threshold D/T value) removal was around 97.6% and the D/T were 1303 and 30.9, respectively, for the influent, and scrubber effluent.
Using double packed towers to deal with coal tar odorous, result from the test indicated that 70-75 and 94.4% of VOCs and odorous intensity in the influent gas could be removed, respectively, with the operation of an initial sodium hypochlorite concentration of 450 mg Cl2/L with pH of 6, combined with a hydrogen peroxide concentration of 4000 mg/L with pH of 9 , VOCs (methane equivalent) concentrations of 20-30 ppm, gas flow rate of 8 NL/min, and a liquid/gas rate ratio of 0.295 m3/m3. At running 300 minutes can smell much odor than beginning.
Baesd on the results from the pilot study, a full-scale plant with waste gas flow rate 200 m3/min was proposed. It was estimated that the cost is around NT$ 20.9 and 52.2 for treating 1,000 m3 of the emitted gases, respectively, for sodium hypochlorite, and sodium hypochlorite combined with hydrogen peroxide. Efforts should be made by decreasing the cost by other alternative technologies.

Identiferoai:union.ndltd.org:NSYSU/oai:NSYSU:etd-0629110-003825
Date29 June 2010
CreatorsWang, Chia-ying
ContributorsMing-Shean Chou, Mei-Jywan Syu, Ju-Sheng Huang
PublisherNSYSU
Source SetsNSYSU Electronic Thesis and Dissertation Archive
LanguageCholon
Detected LanguageEnglish
Typetext
Formatapplication/pdf
Sourcehttp://etd.lib.nsysu.edu.tw/ETD-db/ETD-search/view_etd?URN=etd-0629110-003825
Rightscampus_withheld, Copyright information available at source archive

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