<p>The purpose of this research experiment was to explore and implement a cost-effective automation solution into a low volume production line for loading parts onto a coordinate measuring machine (CMM) for dimensional inspection. Quality control practices have historically been separated from production process by inspection routines being performed in a controlled lab. The system demonstrated the possibilities of an in-process automation of the quality control process that was feasible to be implemented for small and mid-sized manufacturing companies. The process involved an APSX horizontal injection mold machine dispensing parts onto the conveyor belt. The conveyor belt was controlled by a Phoenix Contact PLC and two line sensors that provided two stopping point for cooldown before inspection. A MyCobot 320-M5 robotic arm was used to select the part off the line and places it into a fixture on a Hexagon coordinate measuring machine (CMM).</p>
Identifer | oai:union.ndltd.org:purdue.edu/oai:figshare.com:article/23782497 |
Date | 02 August 2023 |
Creators | Alexander G Hoang (16677327) |
Source Sets | Purdue University |
Detected Language | English |
Type | Text, Thesis |
Rights | CC BY 4.0 |
Relation | https://figshare.com/articles/thesis/_b_Automation_of_the_Quality_Control_Process_with_the_use_of_robotics_and_a_coordinate_Measuring_Machine_b_/23782497 |
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