The main objective of this diploma thesis is to optimize the high lift device on the wing of the Phoenix Air U-15 ultralight aircraft, so that it complies with the UL-2 regulation regarding the stalling speed – 65 KPH. This is fulfilled by optimization of the slotted flap position. Methods used include the Response Surface Method and the Computational Fluid Dynamics approach – namely Ansys Fluent v6 software package. Furthermore, the paper deals with take-off flap optimization and construction of the flap deflection mechanism.
Identifer | oai:union.ndltd.org:nusl.cz/oai:invenio.nusl.cz:228790 |
Date | January 2009 |
Creators | Dvořák, Petr |
Contributors | Šošovička, Róbert, Popela, Robert |
Publisher | Vysoké učení technické v Brně. Fakulta strojního inženýrství |
Source Sets | Czech ETDs |
Language | Czech |
Detected Language | English |
Type | info:eu-repo/semantics/masterThesis |
Rights | info:eu-repo/semantics/restrictedAccess |
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