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Experimental investigation on continuous reinforced SCC deep beams and Comparisons with Code provisions and models

Yes / The test results on eight two-span deep beams made of self-compacting concrete (SCC) are presented and discussed in this paper. The main parameters investigated were the shear span-to-depth ratio, and the amount and configuration of steel reinforcement. All beams failed due to a major diagonal crack formed between the applied mid-span load and the intermediate support separating the beam into two blocks: the first one rotated around the end support leaving the other block resting on the other two supports. Both concrete compressive strength and web reinforcement had a major effect in controlling the shear capacity of the beams tested. For the shear span-to-depth ratio considered, the vertical web reinforcement had more influence on the shear capacity of the specimens than the horizontal web reinforcement. The shear provisions of the ACI 318M-11 are unconservative for most of the beams tested. Comparisons of test results with the strut-and-tie model (STM) suggested by ACI 318M-11, EC2 and CSA23.4-04 showed that the predictions are reasonable for continuous deep beams made with low and medium compressive strength. Although the equation suggested by ACI 318M-11 is very simple, its prediction is more accurate than the STM suggested by different design codes. / This research investigation was funded by the Higher Education Ministry in The Libyan Government.

Identiferoai:union.ndltd.org:BRADFORD/oai:bradscholars.brad.ac.uk:10454/10890
Date14 November 2016
CreatorsKhatab, Mahmoud A.T., Ashour, Ashraf, Sheehan, Therese, Lam, Dennis
Source SetsBradford Scholars
LanguageEnglish
Detected LanguageEnglish
TypeArticle, Accepted Manuscript
Rights© 2016 Elsevier. Reproduced in accordance with the publisher's self-archiving policy. This manuscript version is made available under the CC-BY-NC-ND 4.0 license http://creativecommons.org/licenses/by-nc-nd/4.0/

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