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Feasibility Study of Consolidation by Direct Compaction and Friction Stir Processing of Commercially Pure Titanium Powder

Commercially pure titanium can take up to six months to successfully manufacture a six-inch in diameter ingot in which can be shipped to be melted and shaped into other useful components. The applications to the corrosion-resistant, light weight, strong metal are endless, yet so is the manufacturing processing time. At a cost of around $80 per pound of certain grades of titanium powder, the everyday consumer cannot afford to use titanium in the many ways it is beneficial simply because the number of processing steps it takes to manufacture consumes too much time, energy, and labor. In this research, the steps it takes from the raw powder form to the final part are proposed to be reduced from 4-8 steps to only 2 steps utilizing a new technology that may even improve upon the titanium properties at the same time as it is reducing the number of steps of manufacture. The two-step procedure involves selecting a cylindrical or rectangular die and punch to compress a small amount of commercially pure titanium to a strong-enough compact for transportation to the friction stir welder to be consolidated. Friction stir welding invented in 1991 in the United Kingdom uses a tool, similar to a drill bit, to approach a sample and gradually plunge into the material at a certain rotation rate of between 100 to 2,100 RPM. In the second step, the friction stir welder is used to process the titanium powder held in a tight holder to consolidate into a harder titanium form. The resulting samples are cut to expose the cross section and then grinded, polished, and cleaned to be observed and tested using scanning electron microscopy (SEM), electron dispersive spectroscopy (EDS), and a Vickers microhardness tester. The results were that the thicker the sample, the harder the resulting consolidated sample peaking at 2 to 3 times harder than that of the original commercially pure titanium in solid form at a peak value of 435.9 hardness and overall average of 251.13 hardness. The combined results of the SEM and EDS have shown that the mixing of the sample holder material, titanium, and tool material were not of a large amount and therefore proves the feasibility of this study. This study should be continued to lessen the labor, energy, and cost of the production of titanium to therefore allow titanium to be improved upon and be more efficient for many applications across many industries.

Identiferoai:union.ndltd.org:unt.edu/info:ark/67531/metadc862720
Date08 1900
CreatorsNichols, Leannah Marie
ContributorsFortier, Aleksandra, Horne, Kyle, Mishra, Rajiv
PublisherUniversity of North Texas
Source SetsUniversity of North Texas
LanguageEnglish
Detected LanguageEnglish
TypeThesis or Dissertation
FormatText
RightsPublic, Nichols, Leannah Marie, Copyright, Copyright is held by the author, unless otherwise noted. All rights Reserved.

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