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The effect of condenser backpressure on station thermal efficiency : Grootvlei Power Station as a case study / Kathryn Marie-Louise van RooyenVan Rooyen, Kathryn Marie-Louise January 2014 (has links)
Grootvlei Power Station’s thermal efficiency had been on a steady declining trend since it was re-commissioned in 2008, which had tremendous financial implications to the company at the time of writing. The main contributory factor to the thermal efficiency losses was identified to be the condenser backpressure losses that the station was experiencing. This loss was responsible for approximately 17% of the total efficiency losses. Therefore an investigation was conducted to determine the potential impact of the condenser backpressure loss on the thermal efficiency and the financial implications thereof. The deliverables were to determine the cause of the condenser backpressure loss and propose possible resolutions, to quantify the financial effect and to produce a cost benefit analysis in order to justify certain corrective actions.
Grootvlei Power Station is one of the older power stations in South Africa and it was used as the first testing facility for dry-cooling in South Africa. It consists of six 200MW units, two of which are dry-cooled units. In 1990 it was mothballed and due to rising power demands in South Africa, it was re-commissioned in 2008. Thermal efficiency has been playing a great role due to the power constraints and therefore it was deemed necessary to conduct this study.
The approach that was used was one of experimental and quantitative research and analyses, incorporating deductive reasoning in order to test various hypotheses of factors that could have been contributing to the backpressure losses. In order to do so, a logic diagram was designed which could be used to aid in the identification of possible causes of the condenser backpressure losses. The logic diagram was able to identify whether the problem had to do with the cooling tower or the condenser. It was able to identify which area on the condenser was defective i.e. whether the pumps were not performing, or whether the air ejectors were not performing. It was also able to indicate whether the inefficiency was due to air ingress or fouling.
Alongside the logic diagram, a condenser efficiency analysis was used in order to strengthen and improve on the investigation. This analysis was able to identify whether the condenser was experiencing fouling conditions, air ingress, passing valves or low cooling water flow.
After the investigation commenced, it was decided to focus on the two largest contributing units since the largest contributor was a dry-cooled unit and the second largest contributor was a wet-cooled unit, thus some comparison between the units was incorporated.
The condenser efficiency analysis on Unit 3 (wet-cooled unit) indicated a low cooling water flow, fouling as well as air ingress. The logic diagram indicated poor cooling tower performance, high air ingress as well as fouling. Further tests and analyses as well as visual inspections confirmed these phenomena and condenser fouling was identified to be the largest contributor to the backpressure loss on this unit.
The condenser efficiency analysis on Unit 6 indicated that air was entering the condenser. The logic
diagram indicated that a segment of the backpressure loss was due to poor cooling tower performance.
Inspection of the cooling tower indicated damage and leaks. A cooling tower performance test was
conducted and the result of the test indicated that the tower was in need of cleaning. Further analyses
according to the logic diagram indicated that the condenser was experiencing air ingress which concurred
with the condenser efficiency analysis. A helium test, condensate extraction pump pressure test as well as
a flood test was conducted on this unit and various air in-leakage points were identified.
The financial implications of the backpressure losses were investigated and found to be costing millions
each month. The condenser backpressure loss was contributing more than 2% to the thermal efficiency
loss. The cost benefit analysis indicated that the cost of cleaning the condenser on Unit 3 would be made
up within six months and a return on investment of 16,6% was calculated. The cost benefit analysis
motivates for extended outage times for the purpose of cleaning the condensers from a financial
perspective.
Therefore, it was recommended to clean the condenser on Unit 3 and fix all known defects on the unit as
well as on Unit 6. The cooling towers were recommended to be refurbished. Further investigation was
recommended to determine the feasibility of installing an online cleaning system on the wet-cooled units’
condensers such as a Taprogge system. Alternative investigation methods were suggested such as smoke
stick analyses for air ingress determination. It was also recommended to review the maintenance strategies
that were being used since many of the defects were found to be maintenance related.
If the identified problem areas are attended to, the condenser backpressure loss will decrease and the
condensers transfer heat more efficiently which will lead to financial gains for Grootvlei Power Station as
well as efficiency gains, plant reliability and availability gains. / MIng (Development and Management Engineering), North-West University, Potchefstroom Campus, 2015
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The effect of condenser backpressure on station thermal efficiency : Grootvlei Power Station as a case study / Kathryn Marie-Louise van RooyenVan Rooyen, Kathryn Marie-Louise January 2014 (has links)
Grootvlei Power Station’s thermal efficiency had been on a steady declining trend since it was re-commissioned in 2008, which had tremendous financial implications to the company at the time of writing. The main contributory factor to the thermal efficiency losses was identified to be the condenser backpressure losses that the station was experiencing. This loss was responsible for approximately 17% of the total efficiency losses. Therefore an investigation was conducted to determine the potential impact of the condenser backpressure loss on the thermal efficiency and the financial implications thereof. The deliverables were to determine the cause of the condenser backpressure loss and propose possible resolutions, to quantify the financial effect and to produce a cost benefit analysis in order to justify certain corrective actions.
Grootvlei Power Station is one of the older power stations in South Africa and it was used as the first testing facility for dry-cooling in South Africa. It consists of six 200MW units, two of which are dry-cooled units. In 1990 it was mothballed and due to rising power demands in South Africa, it was re-commissioned in 2008. Thermal efficiency has been playing a great role due to the power constraints and therefore it was deemed necessary to conduct this study.
The approach that was used was one of experimental and quantitative research and analyses, incorporating deductive reasoning in order to test various hypotheses of factors that could have been contributing to the backpressure losses. In order to do so, a logic diagram was designed which could be used to aid in the identification of possible causes of the condenser backpressure losses. The logic diagram was able to identify whether the problem had to do with the cooling tower or the condenser. It was able to identify which area on the condenser was defective i.e. whether the pumps were not performing, or whether the air ejectors were not performing. It was also able to indicate whether the inefficiency was due to air ingress or fouling.
Alongside the logic diagram, a condenser efficiency analysis was used in order to strengthen and improve on the investigation. This analysis was able to identify whether the condenser was experiencing fouling conditions, air ingress, passing valves or low cooling water flow.
After the investigation commenced, it was decided to focus on the two largest contributing units since the largest contributor was a dry-cooled unit and the second largest contributor was a wet-cooled unit, thus some comparison between the units was incorporated.
The condenser efficiency analysis on Unit 3 (wet-cooled unit) indicated a low cooling water flow, fouling as well as air ingress. The logic diagram indicated poor cooling tower performance, high air ingress as well as fouling. Further tests and analyses as well as visual inspections confirmed these phenomena and condenser fouling was identified to be the largest contributor to the backpressure loss on this unit.
The condenser efficiency analysis on Unit 6 indicated that air was entering the condenser. The logic
diagram indicated that a segment of the backpressure loss was due to poor cooling tower performance.
Inspection of the cooling tower indicated damage and leaks. A cooling tower performance test was
conducted and the result of the test indicated that the tower was in need of cleaning. Further analyses
according to the logic diagram indicated that the condenser was experiencing air ingress which concurred
with the condenser efficiency analysis. A helium test, condensate extraction pump pressure test as well as
a flood test was conducted on this unit and various air in-leakage points were identified.
The financial implications of the backpressure losses were investigated and found to be costing millions
each month. The condenser backpressure loss was contributing more than 2% to the thermal efficiency
loss. The cost benefit analysis indicated that the cost of cleaning the condenser on Unit 3 would be made
up within six months and a return on investment of 16,6% was calculated. The cost benefit analysis
motivates for extended outage times for the purpose of cleaning the condensers from a financial
perspective.
Therefore, it was recommended to clean the condenser on Unit 3 and fix all known defects on the unit as
well as on Unit 6. The cooling towers were recommended to be refurbished. Further investigation was
recommended to determine the feasibility of installing an online cleaning system on the wet-cooled units’
condensers such as a Taprogge system. Alternative investigation methods were suggested such as smoke
stick analyses for air ingress determination. It was also recommended to review the maintenance strategies
that were being used since many of the defects were found to be maintenance related.
If the identified problem areas are attended to, the condenser backpressure loss will decrease and the
condensers transfer heat more efficiently which will lead to financial gains for Grootvlei Power Station as
well as efficiency gains, plant reliability and availability gains. / MIng (Development and Management Engineering), North-West University, Potchefstroom Campus, 2015
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Efficiency of a direct contact condenser in the presence of the noncondensable gas air compared to a tube and shell condenserLebsack, Jonathan M. 20 March 2012 (has links)
Steam distillation is the traditional method used for the extraction of peppermint oil. This process is able to remove approximately 20% of the oils from the leaves of the plant. It is a very costly and un-sustainable process due to the release of carbon emissions. Solvent free microwave extraction promises yields of up to 65% of the "available" oils from the peppermint at 3% less cost (Velasco 2007). It can also reduce carbon emissions because it will be using electricity as a power source instead of fossil fuels, however not all electric companies use renewable energies. In 2009 a SFME pilot plant was assembled in North Carolina to test the efficiency of the microwave process on a larger than lab scale. Results from the experiments showed that the tube and shell condenser was unable to effectively condense the mint oil. The problem was determined to be the addition of air to the mixture due to the open ends of the microwave. However it was discovered that the spray scrubber after the condenser was able to collect a visible amount of oil. This inspired the design of a
direct contact condenser (Pommerenck 2012). The direct contact condenser they designed, built, and tested showed vast improvements in steam capturing efficiency when compared to a tube and shell condenser. However due to the materials used for its construction it could not sustain operating temperatures seen in the microwave pilot plant. Using their design a new direct contact condenser was built using materials that would be able to withstand heavy temperatures. The condenser was constructed out of aluminum and contained stainless steel spray nozzles, both for their non-corrosive properties. Tests were conducted using 8 and 16 nozzles and tested over a range of 20-100% steam by mass. Additional tests were completed using the full 24 nozzles but due to the location of some of the nozzles coolant was lost as an aerosol with no way to quantify the loss. Comparing the data to research completed by Pommerenck et al. on efficiency of a tube and shell condenser used for the mint distillation process found that with increasing amounts of air there is a greater loss of heat transfer. This is believed to be the effects of a boundary layer of the noncondensable fluid, air, which forms along the tube and resists condensation from forming (Seunguim 2006). Pommerenck's tube and shell condenser used a coolant flow rate of 24 L/min while the flow rates tested in this research were 18 L/min and 36 L/min. The direct contact condenser showed a considerable increase in performance even with the smaller flow rate compared to the tube and shell unit, indicating removal of the boundary layer. The efficiency tends to follow the maximum theoretical efficiency while the tube and shell condenser lowers in efficiency. The overall goal of this project is to determine the feasibility of the use of a direct contact condenser for implementation in the solvent free microwave extraction of peppermint oil when air is present. / Graduation date: 2012
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