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Desempenho e caracterização microbiana do processo de dois estágios com reatores anaeróbios de fluxo ascendente com manta de lodo (UASB) tratando águas residuárias de suinocultura / Performance and microbial characterization of the two stage process with upflow anaerobic sludge blanket reactors (UASB) treating swine wastewaterPereira, Edson Rivelino 04 February 2004 (has links)
Foram operados dois reatores UASB de bancada (volumes de 39,0 e 10,5 L) instalados em série, alimentados com águas residuárias de suinocultura com concentração de sólidos suspensos totais (SST), no primeiro reator, em torno de 5000 mg/L, com temperatura controlada (de 25 a 30 graus Celsius) e com tempo de detenção hidráulica (TDH) no primeiro reator de 62 a 16 h e no segundo de 16 a 4 h. O objetivo foi avaliar o desempenho e caracterizar física e microbiologicamente o lodo dos reatores UASB operados em dois estágios. Os resultados obtidos no ensaio 1, com TDH de 62 h no primeiro reator e SST no afluente de 5240 mg/L, mostraram eficiências de remoção de DQO total de 86% e 59% e SST de 82% e 57%, no primeiro e segundo reatores, respectivamente. A eficiência de remoção de DQO total e SST no sistema, no ensaio 1, foi de 95% e 94%. No ensaio 2, com TDH de 31 h no primeiro reator e SST de 5000 mg/L no afluente, observou-se eficiência de remoção de DQO total de 86% e 43% e SST de 85% e 58%, no primeiro e segundo reatores, respectivamente. A eficiência de remoção de DQO total e SST no sistema, no ensaio 2, foi de 92% e 94%. No ensaio 3, com TDH de 16 h no primeiro reator e SST de 5490 mg/L no afluente, observou-se eficiência de remoção de DQO total de 73% e 23% e SST de 65% e 20%, no primeiro e segundo reatores, respectivamente. A eficiência de remoção de DQO total e SST no sistema, no ensaio 3, foi de 79% e 73%. A TCOV aplicada no primeiro reator, no ensaio 1, foi de 4,55 kg DQO total/\'M POT.3\'.d, no ensaio 2 de 8,75 kg DQO total/\'M POT.3\'.d e no ensaio 3 de 18,65 kg DQO total/\'M POT.3\'.d. A produção de \'CH IND.4\' no primeiro reator foi de 17,50 a 68,20 L \'CH IND.4\'/d e no segundo reator de 1,62 a 5,50 L \'CH IND.4\'/d com a diminuição do TDH. Os reatores UASB instalados em série foram eficientes na remoção da fração dissolvida e, principalmente, da fração devido à concentração de SST do afluente. Para TCOV de 4,55 kg DQO/\'M POT.3\'.d no primeiro reator, pôde-se obter eficiências de remoção de DQO total e de SST acima de 90% e de DQO dissolvida acima de 85%. Para TCOV de 18,65 kg DQO/\'M POT.3\'.d no primeiro reator, as eficiências de remoção de DQO total e de SST foram acima de 70% e DQO dissolvida acima de 75%. As maiores produções específicas de metano foram obtidas com TCOV de 2,55 kg DQO/\'M POT.3\'.d para o segundo reator e de 8,65 kg DQO/\'M POT.3\'.d para o primeiro reator. A operação dos reatores UASB com valores de concentração de SST no afluente em torno de 5000 mg/L foram prejudiciais ao processo de granulação do lodo. Os grânulos apresentaram distribuição dispersa das morfologias microbianas ao longo da parede, não caracterizando a divisão em camadas definidas. As arqueas metanogênicas predominantes foram as semelhantes à Methanosaeta. / Two bench scale UASB reactors (volumes of 39,0 and 10,5 L) were operated in sequence, fed with swine wastewater with total suspended solids (TSS) concentration around 5000 mg/L in the first reactor, with controlled temperature (from 25 to 30 Celsius degrees) and operating with hydraulic detention time (HDT) in the first reactor varying from 62 to 16 h and in the second reactor from 16 to 4 h. The objective was to evaluate the performance and to characterize physically and microbiologically the sludge from UASB reactors operated in two stages treating swine wastewater. The results obtained in phase 1, with HDT of 62 h in the first reactor and TSS in the influent of 5240 mg/L, presented total COD removal efficiencies of 86% and 59% and TSS reduction efficiency of 82% and 57%, in the first and second reactors, respectively. The removal efficiency of total COD and TSS in the system, in phase 1, was 95% and 94%, respectively. In the phase 2, using HDT of 31 h in the first reactor and TSS of 5000 mg/L in the influent, it was observed a total COD removal efficiency of 86% and 43% and TSS reduction efficiency of 85% and 58%, in the first and second reactors, respectively. The system removal efficiency of total COD and TSS in phase 2, was 92% and 94%, respectively. In phase 3, with a HDT of 16 h in the first reactor and TSS of 5490 mg/L in the influent, it was observed a total COD removal efficiency of 73% and 23% and TSS reduction efficiency of 65% and 20%, in the first and second reactors, respectively. The total COD removal efficiency and TSS reduction efficiency in the system, in phase 3, was 79% and 73%, respectively. The volumetric organic loading rate (VOLR) applied in the first reactor, in phase 1, was 4,55 kg total COD/\'M POT.3\'.d, in phase 2 was 8,75 kg total COD/\'M POT.3\'.d and in phase 3 was 18,65 kg total COD/\'M POT.3\'.d. The \'CH IND.4\' production in the first reactor was from 17,50 to 68,20 L \'CH IND.4\'/d and in the second reactor from 1,62 to 5,50 L \'CH IND.4\'/d decreasing the HDT in the experiment phases. The UASB reactor installed in sequence were efficient in the dissolved fraction removal and, mainly, to the fraction due to the TSS influent concentration. The total VOL value of 4,55 kg COD/\'M POT.3\'.d was measured in the first reactor, it was achieved TSS and total COD removal efficiencies above 90% and dissolved COD above 85%. For the OVL of 18,65 kg COD/\'M POT.3\'.d in the first reactor the TSS and total COD removal were above 70% and dissolved COD above 75%. The larger methane specific production was obtained with a total VOL of 2,55 kg COD/\'M POT.3\'.d in the second reactor and 8.65 kg COD/\'M POT.3\'.d in the first reactor. The UASB reactors operation with the TSS concentration values of 5000 mg/L in the influent was prejudicing the sludge granulation process. The granules present a microbial morphology disperse distribution that doesn\'t characterize a layers defined distribution. The predominant metonogenic archeas were similar to Methanosaeta.
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Desempenho e caracterização microbiana do processo de dois estágios com reatores anaeróbios de fluxo ascendente com manta de lodo (UASB) tratando águas residuárias de suinocultura / Performance and microbial characterization of the two stage process with upflow anaerobic sludge blanket reactors (UASB) treating swine wastewaterEdson Rivelino Pereira 04 February 2004 (has links)
Foram operados dois reatores UASB de bancada (volumes de 39,0 e 10,5 L) instalados em série, alimentados com águas residuárias de suinocultura com concentração de sólidos suspensos totais (SST), no primeiro reator, em torno de 5000 mg/L, com temperatura controlada (de 25 a 30 graus Celsius) e com tempo de detenção hidráulica (TDH) no primeiro reator de 62 a 16 h e no segundo de 16 a 4 h. O objetivo foi avaliar o desempenho e caracterizar física e microbiologicamente o lodo dos reatores UASB operados em dois estágios. Os resultados obtidos no ensaio 1, com TDH de 62 h no primeiro reator e SST no afluente de 5240 mg/L, mostraram eficiências de remoção de DQO total de 86% e 59% e SST de 82% e 57%, no primeiro e segundo reatores, respectivamente. A eficiência de remoção de DQO total e SST no sistema, no ensaio 1, foi de 95% e 94%. No ensaio 2, com TDH de 31 h no primeiro reator e SST de 5000 mg/L no afluente, observou-se eficiência de remoção de DQO total de 86% e 43% e SST de 85% e 58%, no primeiro e segundo reatores, respectivamente. A eficiência de remoção de DQO total e SST no sistema, no ensaio 2, foi de 92% e 94%. No ensaio 3, com TDH de 16 h no primeiro reator e SST de 5490 mg/L no afluente, observou-se eficiência de remoção de DQO total de 73% e 23% e SST de 65% e 20%, no primeiro e segundo reatores, respectivamente. A eficiência de remoção de DQO total e SST no sistema, no ensaio 3, foi de 79% e 73%. A TCOV aplicada no primeiro reator, no ensaio 1, foi de 4,55 kg DQO total/\'M POT.3\'.d, no ensaio 2 de 8,75 kg DQO total/\'M POT.3\'.d e no ensaio 3 de 18,65 kg DQO total/\'M POT.3\'.d. A produção de \'CH IND.4\' no primeiro reator foi de 17,50 a 68,20 L \'CH IND.4\'/d e no segundo reator de 1,62 a 5,50 L \'CH IND.4\'/d com a diminuição do TDH. Os reatores UASB instalados em série foram eficientes na remoção da fração dissolvida e, principalmente, da fração devido à concentração de SST do afluente. Para TCOV de 4,55 kg DQO/\'M POT.3\'.d no primeiro reator, pôde-se obter eficiências de remoção de DQO total e de SST acima de 90% e de DQO dissolvida acima de 85%. Para TCOV de 18,65 kg DQO/\'M POT.3\'.d no primeiro reator, as eficiências de remoção de DQO total e de SST foram acima de 70% e DQO dissolvida acima de 75%. As maiores produções específicas de metano foram obtidas com TCOV de 2,55 kg DQO/\'M POT.3\'.d para o segundo reator e de 8,65 kg DQO/\'M POT.3\'.d para o primeiro reator. A operação dos reatores UASB com valores de concentração de SST no afluente em torno de 5000 mg/L foram prejudiciais ao processo de granulação do lodo. Os grânulos apresentaram distribuição dispersa das morfologias microbianas ao longo da parede, não caracterizando a divisão em camadas definidas. As arqueas metanogênicas predominantes foram as semelhantes à Methanosaeta. / Two bench scale UASB reactors (volumes of 39,0 and 10,5 L) were operated in sequence, fed with swine wastewater with total suspended solids (TSS) concentration around 5000 mg/L in the first reactor, with controlled temperature (from 25 to 30 Celsius degrees) and operating with hydraulic detention time (HDT) in the first reactor varying from 62 to 16 h and in the second reactor from 16 to 4 h. The objective was to evaluate the performance and to characterize physically and microbiologically the sludge from UASB reactors operated in two stages treating swine wastewater. The results obtained in phase 1, with HDT of 62 h in the first reactor and TSS in the influent of 5240 mg/L, presented total COD removal efficiencies of 86% and 59% and TSS reduction efficiency of 82% and 57%, in the first and second reactors, respectively. The removal efficiency of total COD and TSS in the system, in phase 1, was 95% and 94%, respectively. In the phase 2, using HDT of 31 h in the first reactor and TSS of 5000 mg/L in the influent, it was observed a total COD removal efficiency of 86% and 43% and TSS reduction efficiency of 85% and 58%, in the first and second reactors, respectively. The system removal efficiency of total COD and TSS in phase 2, was 92% and 94%, respectively. In phase 3, with a HDT of 16 h in the first reactor and TSS of 5490 mg/L in the influent, it was observed a total COD removal efficiency of 73% and 23% and TSS reduction efficiency of 65% and 20%, in the first and second reactors, respectively. The total COD removal efficiency and TSS reduction efficiency in the system, in phase 3, was 79% and 73%, respectively. The volumetric organic loading rate (VOLR) applied in the first reactor, in phase 1, was 4,55 kg total COD/\'M POT.3\'.d, in phase 2 was 8,75 kg total COD/\'M POT.3\'.d and in phase 3 was 18,65 kg total COD/\'M POT.3\'.d. The \'CH IND.4\' production in the first reactor was from 17,50 to 68,20 L \'CH IND.4\'/d and in the second reactor from 1,62 to 5,50 L \'CH IND.4\'/d decreasing the HDT in the experiment phases. The UASB reactor installed in sequence were efficient in the dissolved fraction removal and, mainly, to the fraction due to the TSS influent concentration. The total VOL value of 4,55 kg COD/\'M POT.3\'.d was measured in the first reactor, it was achieved TSS and total COD removal efficiencies above 90% and dissolved COD above 85%. For the OVL of 18,65 kg COD/\'M POT.3\'.d in the first reactor the TSS and total COD removal were above 70% and dissolved COD above 75%. The larger methane specific production was obtained with a total VOL of 2,55 kg COD/\'M POT.3\'.d in the second reactor and 8.65 kg COD/\'M POT.3\'.d in the first reactor. The UASB reactors operation with the TSS concentration values of 5000 mg/L in the influent was prejudicing the sludge granulation process. The granules present a microbial morphology disperse distribution that doesn\'t characterize a layers defined distribution. The predominant metonogenic archeas were similar to Methanosaeta.
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