• Refine Query
  • Source
  • Publication year
  • to
  • Language
  • 1
  • Tagged with
  • 4
  • 4
  • 2
  • 2
  • 2
  • 1
  • 1
  • 1
  • 1
  • 1
  • 1
  • 1
  • 1
  • 1
  • 1
  • About
  • The Global ETD Search service is a free service for researchers to find electronic theses and dissertations. This service is provided by the Networked Digital Library of Theses and Dissertations.
    Our metadata is collected from universities around the world. If you manage a university/consortium/country archive and want to be added, details can be found on the NDLTD website.
1

The tribology of the overhead cam train in automobile

Smarajit, R. January 1987 (has links)
No description available.
2

Improving the performance of internal combustion engines through lubricant engineering

Taylor, Oliver January 2016 (has links)
Low friction lubricant development provides a worthwhile contribution to vehicle CO<sub>2</sub> emission reduction. Conventional low friction lubricant development focuses on empirical processes using out dated engine technology and old test methods. This strategy is inefficient and restricts the lubricant's potential. A new method proposed in the present research combines tribological simulations with rig, engine and vehicle tests. This approach provides insights undocumented until now. The contribution to CO<sub>2</sub> emission reduction from individual engine components on vehicle drive cycles that include warm-up is predicted using lubricants down to the new SAE 8 viscosity grade. A bearing model is used to design the lubricant's non Newtonian characteristics to achieve friction reduction. An isoviscous lubricant with a viscosity of 4.6 cSt is shown to achieve the minimum friction in the bearing. The research shows that by starting with lubricants having kinematic viscosities higher than this value, it is possible to improve lubricant performance by lowering viscosity index (VI), introducing shear thinning, or reducing the density and pressure viscosity coefficient. Conversely, for lubricants with lower starting viscosities it is shown that higher VI values, more shear-stable lubricants and higher densities and pressure viscosity coefficients are required. The model predicts that high oil film pressures occur in the bearing and cause significant local lubricant viscosity increase (300&percnt;), indicating that the lubricant's pressure viscosity behaviour is important here, despite the contact being conformal. Simulation and motored engine testing establishes lubricant behaviour in the piston-to-bore conjunction. This analysis identifies a poor correlation between measured and predicted values at low engine speeds. A rig-on-liner tribometer shows that this error is attributable to a deficiency in the simulation's characterisation of boundary regime friction. An oil pump test determines how a modern variable displacement oil pump (and its control system) responds to lowering viscosity. The hypothesis that low viscosity lubricants cause the parasitic load from this component to increase is disproven using this component-level rig test. Chassis dynamometer testing compares the CO<sub>2</sub> reduction performance of lubricant thermal management systems to the values achieved by reducing the viscosity grade. CO<sub>2</sub> reductions of between 0.4&percnt; and 1.0&percnt; are identified using a cold-start new European drive cycle (NEDC) with a 5W-30 preheated to 60&deg;C and 90&deg;C respectively. Reductions in CO<sub>2</sub> emissions between 0.4&percnt; and 1.2&percnt; are found on the NEDC by lowering the oil fill volume from 5.1 L to 2.1 L. For the unmodified case, a 3.7&percnt; reduction in CO<sub>2</sub> emissions is reported by reducing the viscosity grade from a 5W 30 to an SAE 8 in the NEDC. The performance of a novel external oil reservoir is simulated to understand its ability to retain oil temperature during the vehicle cool-down procedure. An oil temperature of 65&deg;C at the end of the soak period (following a prior test where the oil was assumed to reach 90&deg;C) is predicted by installing insulation to the reservoir and indicates that a viable method to achieve the CO<sub>2</sub> benefits identified through lubricant preheating tests exists. A full vehicle model combines the outputs from each of these sub-models to predict lubricant performance on the NEDC the new World-wide harmonized light duty test cycle (WLTC). This new approach provides a tool that enables next generation low friction lubricants to be developed. The model predicts that an SAE 8 lubricant can reduce CO2 emissions by 2.8&percnt; on the NEDC and 1.9&percnt; on the WLTC compared to a 5W-30. A theoretical experiment, where all lubricant related friction was deleted from the simulation, predicts that lubricant-related CO<sub>2</sub> emissions are 8.7&percnt; on the NEDC and reduce to 6.3&percnt; on the WLTC. These results indicate that the planned adoption of the WLTC in September 2017 reduces the potential contribution to CO<sub>2</sub> emission reduction from lubricants by 28&percnt;.
3

Pretreatment of Small Four-Stroke Engine Components for No-Oil Hot Tests

Talluri, Srikrishna 13 December 2000 (has links)
"Hot-tests" form a vital facet towards the end of the production line of modern automotive plants, where the condition of the engine is checked by running it for a short period of time, to ensure its performance under standard operating conditions. The duration of hot-tests for small engines varies from 20-75 seconds. In the conventional procedure, about 10-30 grams of lubricant (for pre-coating) is used with about 650ml of standard oil for engine testing. However, about 1-3 oz. of oil is lost per engine, as it cannot be sucked out of the crankcase after the hot tests. The loss of 1-3 oz. of oil leads to a significant loss in revenue, over the large number of engines manufactured. It also causes a potential safety and environmental hazard due to leakage of lubricant during shipping or upon first use in a particular application. The goal of this project is to conduct "no-oil" hot tests using less than 10 grams of specially formulated lubricants for pretreatment. Implementation of this procedure for conducting the hot tests in the manufacturing facility would save revenue and eliminate potential hazards mentioned above in addition to cutting down on manpower and/or machinery used for handling the engine oil. An experimental study of pre-treatment of interacting interfaces of engine components, with specially formulated lubricants, for no-oil hot tests is presented. This study includes sixteen tests performed on the production line of Tecumseh's small engine manufacturing plant. The formulated lubricants were made up of tribopolymer formers, i.e., monomers, which were used in previous tribopolymerization studies. Tribopolymerization is defined as the planned or intentional formation of protective polymeric films directly and continuously on rubbing surfaces to reduce damage and wear by the use of minor concentrations of selected compounds capable of forming polymeric films in situ. This study entailed the investigation of the anti-wear properties of the formulated lubricants on a high temperature pin-on-disk machine and subsequent selection of lubricants exhibiting superior performance for use in the engine tests. The no-oil hot-tests performed at Virginia Tech and on the assembly line exhibited the superior anti-scuffing/anti-wear properties of the specially formulated lubricants, to warrant their use on the production line in the near future. / Master of Science
4

Konstrukce bloku motoru leteckého motoru / Engine Block Design of Aircraft Powertrain

Kuzník, Bořek January 2013 (has links)
This thesis describes the problems of the engine block and crankcase. There is solution of structural design and contains the engineering design of invert six-cylinder engine block with water cooling. Thesis deals with connected equipment and drives. Engineering design is verified by finite elements analysis for the determination of strenght and durability. The ending of thesis analyzes the production methods of designed engine block.

Page generated in 0.0817 seconds