M.Ing. / Columbus Stainless, a subsidiary of Acerinox, manufactures stainless steel in their plant located in Middelburg, South Africa. During the hot rolling operation the steel is rolled on a 4-high finishing mill where strip movement perpendicular to the rolling direction occurs. This movement is undesirable because it causes inferior product quality and may also lead to downtime if the strip moves past the edge of the rolls. In the past the operator made adjustments to the relative alignment of the rolls in the mill in an attempt to limit the sideways movement of the strip. In order to improve product quality and production throughput, the manual action of adjusting the parallelism of the rolls was replaced with an automatic steering control system. Analysis of the process revealed that several variables have an impact on the way the strip reacts to changes in the alignment of rolls in the mill. An adaptive fuzzy logic control system was designed and implemented in the real time control system of the mill. During commissioning the system did not have an adverse effect on production and all initial project criteria were met, as was stipulated in Section 1.4 of this document. The control system improved the strip movement by an average of 11% on various products rolled. Based on production data, the system potentially prevented two coils from leaving the rolls during the month long evaluation period and saved 40 minutes of production time. If the savings in material losses and the potential gain in production time are added the possible anticipated monetary saving is estimated to be about 24 million Rand a year.
Identifer | oai:union.ndltd.org:netd.ac.za/oai:union.ndltd.org:uj/uj:8158 |
Date | 26 February 2009 |
Source Sets | South African National ETD Portal |
Detected Language | English |
Type | Thesis |
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