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The effects of diffusers and aspect ratio on air flow in fan plenumsYeh, Wen-Shu 08 1900 (has links)
No description available.
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Power reduction of mine ventilation fans /Beswick, Michael Unknown Date (has links)
Thesis (MEng)--University of South Australia, 1998
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Power reduction of mine ventilation fans /Beswick, Michael Unknown Date (has links)
Thesis (MEng)--University of South Australia, 1998
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Axial-flow fan noise : with particular reference to the noise caused by vortex formation at the trailing edge and upper surface of blades.Gower, Stephen Newman. January 1966 (has links) (PDF)
Thesis (M.E.) -- University of Adelaide, Dept. of Mechanical Engineering, 1968.
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The correlation of randomness with high tip losses in an axial flow fan stage /Alday, John Hane, January 1991 (has links)
Thesis (M.S.)--Virginia Polytechnic Institute and State University, 1991. / Vita. Abstract. Includes bibliographical references (leaves 119-121). Also available via the Internet.
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Feedback applications in active noise control for small axial cooling fans /Green, Matthew J., January 2006 (has links) (PDF)
Thesis (M.S.)--Brigham Young University. Dept. of Physics and Astronomy, 2006. / Includes bibliographical references (p. 67-69).
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Performance measurements, flow visualization, and numerical simulation of a crossflow fanSeaton, M. Scot. 03 1900 (has links)
Approved for public release, distribution unlimited / A 12-inch diameter, 1.5-inch span crossflow fan test apparatus was constructed and tested using the existing Turbine Test Rig (TTR) as a power source. Instrumentation was installed and a data acquisition program was developed to measure the performance of the crossflow fan. Performance measurements were taken over a speed range of 1,000 to 7,000 RPM. Results comparable to those measured by Vought Systems Division of LTV Aerospace in 1975 were obtained. At 6,000 RPM, a thrust-to-power ratio of one was determined; however, at 3,000 RPM twice the thrust-to-power ratio was measured. Flow visualization was conducted using dye-injection methods. Performance and flow visualization results were compared to predictions obtained from 2-D numerical simulation conducted using Flo++, a commercial PC-based computational fluid dynamics software package by Softflo. A possible design for a light civil V/STOL aircraft was suggested using a similar crossflow fan apparatus for both lift and propulsion. / Lieutenant, United States Navy
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Performance measurements, flow visualization, and numerical simulation of a crossflow fan /Seaton, M. Scot. January 2003 (has links) (PDF)
Thesis (M.S. in Aeronautical Engineering)--Naval Postgraduate School, March 2003. / Thesis advisor(s): Garth V. Hobson, Raymond P. Shreeve. Includes bibliographical references (p. 69-70). Also available online.
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Fan noise reduction from a supersonic inlet /Nuckolls, William E., January 1992 (has links)
Thesis (M.S.)--Virginia Polytechnic Institute and State University, 1992. / Vita. Abstract. Includes bibliographical references (leaves 66-67). Also available via the Internet.
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A study of prerotation in the inlet duct of a centrifugal fanRodenkirch, Norman Edward, January 1966 (has links)
Thesis (M.S.)--University of Wisconsin--Madison, 1966. / eContent provider-neutral record in process. Description based on print version record. Includes bibliographical references.
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