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Application of analytical chemistry to waste minimisation in the powder coating industry.January 2005 (has links)
A local company instituted a new chemical procedure in their spray phosphating system
used in the pretreatment of large components for industrial racking systems. An inorganic
conversion coating is deposited on the workpiece surface during phosphating and this
prepares the surface to receive an organic top-coat. The organic coating is applied to the
workpiece surface in the form of a powder and cured to form a continuous film about 80
u.m thick.
The solution chemistry of the phosphating system was monitored by sampling and
chemical analysis and taking direct reading instrumental measurements on the process
and rinse solutions. The process was also evaluated using the results of a waste
minimisation audit. This involved gathering data on composition, flow rates and costs of
inputs and outputs of the process. Two types of information were collected and used
during the audit, namely chemical monitoring (concentration levels of Na, Fe, Zn, Mo,
Mn and Cr and measurements of conductivity, TDS, SS and pH) and water usage data on
the Phosphating Line and existing data (raw materials, workpieces and utility inputs as
well as domestic waste, factory waste and scrap metal outputs). The data were analysed
using four established waste minimisation techniques. The Scoping Audit and the Water
Economy Assessment results were determined using empirically derived models. The
Mass Balance and the True Cost of Waste findings were obtained through more detailed
calculations using the results of the chemical analysis.
The results of the audit showed that the most important area for waste minimsation in the
Phosphating Line was the (dragged-out phosphating chemicals present in) wastewater
stream. According to the scoping audit, water usage had the third highest waste
minimisation potential behind powder and steel consumption for the entire powder
coating process. While the scoping audit and the specific water intake value showed that
water consumption for the process was not excessive, it did not indicate that the pollution
level in the rinse waters was high. Further, drag-out calculations showed that drag-out
volumes were typical of those found in the metal finishing industry. However the presence of high levels of metal species in the rinse waters was highlighted through the
chemical monitoring of the Phosphating Line. The True Cost of Waste Analysis
estimated potential financial savings for the effluent stream at about R8000 for a period
of 105 days. However this does not take into consideration the cost of the liability
associated with this stream when exceeding effluent discharge limits (given in the Trade
Effluent Bylaws) or of the chemical treatment necessary to render this stream suitable for
discharge to sewer. Intervention using only "low-cost-no-cost" waste minimisation
measures was recommended as a first step before contemplating further areas for
technical or economic feasibility studies. However, a further study involving monitoring
the sludge was recommended in order to establish the potential financial savings offered
by this waste stream. / Thesis (M.Sc.)-University of KwaZulu-Natal, Pietermaritzburg, 2005.
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An assessment of the Pietermaritzburg Waste Minimisation Club and the waste minimisation opportunities on a coil coating plant.January 2002 (has links)
This study involved an assessment of the Pietermaritzburg Waste Minimisation Club (PWMC) during 2001, and a waste minimisation audit conducted at two coil coating lines. Waste minimisation is the reduction or elimination of waste at source4 • It is often achieved
through waste minimisation clubs which comprise a small number of companies, generally in the same geographicaI area, that are interested in reducing waste 1"711 .
The success of the PMWC was evaluated in terms of the degree to which members implemented waste minimisation principles. Two questionnaires were used to assess the success of the club. These indicated that although the training material gave the members a good understanding of the basic principles of waste minimisation, the material has not given
the members enough practical information to implement a waste minimisation programme in their companies. The main barriers to waste minimisation identified include production pressure, operational constraints, lack of human resources and a lack of management time.
The drivers for waste minimisation were financial savings, improved plant utilisation and improved environmental performance.
Coil coating is a continuous process where a coiled sheet of aluminium is cleaned, pretreated and coated with paint. The flow rates, compositions and costs of all input and output streams to the cleaning and pretreatment sections were gathered from operators or measured. The data
were collected over a three-month period to obtain a representative sample, and then analysed to determine waste minimisation opportunities using mass balances, monitoring and targeting, a scoping audit and a true cost of waste assessment. The scoping audit was found to be the
most useful technique because it accurately prioritised the waste minimisation opportunities but required a relatively small amount of data for its application. However, the scoping audit underestimated the savings that could be achieved at the coil coating department and therefore the 'scope to save' percentages, which were developed for United Kingdom industries, need modification to better reflect South African industry.
Opportunities for waste minimisation on Coil Coating Line 1 (CCL1) included reducing the water consumption, reducing the acid and chromium raw materials consumption, and finding a cheaper energy source for heating the process and rinse tanks. Potential fmancial savings of R116 000 and environmental savings of 18 200 kL of water or effluent per year were
calculated for CCL1.
The chromium and acid effluent treatment and solid waste disposal are the main areas for waste minimisation on Coil Coating Line 2 (CCL2). Savings could be achieved in these areas by using roller application ofthe chromium pretreatment rather than spray application, and by preventing a leak of chromium pretreatment into the acid process and rinse tanks. Other
savings can also be achieved by operating the chromium process tank as a fed-batch process, and operating the alkali and acid process tanks as continuous processes at the specified chemical concentrations and with recycle of the rinse water (dragout). The total financial savings that can be achieved on CCL2 are R5.3 million, and potential environmental savings
are 31 600 kL ofeffluent per year. / Thesis (M.Sc.)- University of Natal, Pietermaritzburg, 2002.
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Análise da influência das condições de corte sobre o fresamento em acabamento de aços endurecidos usando altas velocidades / Analysis of the cutting conditions influence on the finish of hardened steels using high speed millingAguiar, Marcelo Mendes de 02 February 2012 (has links)
Orientador: Anselmo Eduardo Diniz / Dissertação (mestrado) - Universidade Estadual de Campinas, Faculdade de Engenharia Mecânica / Made available in DSpace on 2018-08-19T18:33:44Z (GMT). No. of bitstreams: 1
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Previous issue date: 2012 / Resumo: Normalmente, a utilização de aços ferramenta endurecidos, juntamente com as formas complexas típicas das peças utilizadas na área de moldes e matrizes, oferecem dificuldade na usinagem por fresamento, principalmente nas operações de acabamento que exijam o uso de ferramentas longas. A técnica de fresamento HSM (High Speed Machining - usinagem em altas velocidades, ou ainda High Speed Milling - fresamento em altas velocidades) tem se tornado uma alternativa para realizar este tipo de usinagem, reduzindo, ou às vezes até eliminando operações de eletro-erosão e polimento. Tipicamente, as fresas de pastilhas de metal duro intercambiáveis tem sido usadas em operações de desbaste e semi-acabamento, enquanto nas operações de acabamento ou em usinagem de geometrias que exijam ferramentas com pequenos diâmetros ainda predomina o uso de fresas inteiriças. O objetivo principal deste estudo é avaliar a influência de cinco variáveis de processo de fresamento com alta velocidade de corte, sobre o acabamento da superfície usinada. A influência do desgaste das ferramentas sobre o acabamento superficial, ao longo de 400 minutos de usinagem, também foi avaliado, além de uma comparação entre ferramentas inteiriças de metal duro e ferramentas de pastilha intercambiável montada em corpo de metal duro, a fim de avaliar a viabilidade técnica do uso deste segundo tipo de ferramenta, em substituição às tradicionais fresas inteiriças utilizadas em operações de acabamento. Na maioria dos experimentos realizados, pequenos valores de rugosidade foram mantidos, demonstrando que operações de acabamento em aço ABNT H13 IM com dureza de 50 HRC é possível com vida longa de ferramenta, mesmo utilizando-se valor de 500 m/min para velocidade de corte. Além disto, a análise da influência das variáveis de processo utilizadas neste trabalho mostrou que é possível, sob algumas condições, utilizar tanto ferramentas inteiriças, quanto de pastilha intercambiável montada em corpo de metal duro em operações de acabamento / Abstract: Typically, the use of hardened tool steels, along with complex shapes typical of the parts used in the field of molds and dies, offer difficulty in machining by milling, mainly in finishing operations that demand the use of long tool. The HSM (High Speed Machining or High Speed Milling) has become a possible alternative for making this type of machining, reducing, or sometimes eliminating electric discharge machining and polishing operations. Usually, indexable carbide insert mills has been used for roughing and semi-finishing, while in finishing operations or when the machining geometries that require tools with small diameters the integral tools are used yet. The main objective of this study is to evaluate the influence of five process variables, with high cutting speed, on the finish of the machined surface. The influence of tool wear on surface finish through 400 minutes of milling was also evaluated, as well as a comparison between integral carbide mills and indexable insert mounted at cemented carbide toolholder endmills, in order to evaluate the technical feasibility of using this second type of tool, replacing the traditional integral carbide endmills used in finishing operations. In most experiments, small roughness values were maintained, showing that finishing operations on AISI H13 IM with a hardness of 50 HRC is possible with long tool life, even using the cutting speed of 500 m/min. Furthermore, the analysis of the influence of process variables used in this study showed that is possible, under some conditions, the use either integral carbide tools, or indexable insert mounted at cemented carbide toolholder endmills on finishing operations / Mestrado / Materiais e Processos de Fabricação / Mestre em Engenharia Mecânica
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Phosphate stabilization by non-chromate post-rinse treatmentYoon, Tae-Ho January 1987 (has links)
Zinc phosphate conversion coating has been applied to improve the corrosion resistance and paint adhesion. However, zinc phosphate crystals dissolve in a highly alkaline environment, which reduces the corrosion resistance of base metal. To improve the phosphate stability in a highly alkaline environment, a post-rinse treatment has been applied to phosphate coating by rinsing with an aqueous solution which contains certain anions or cations. Chromatepost-rinse treatment is the most widely used method and has shown a great improvement in corrosion resistance. But, due to the environmental problems caused by chromate ions, non-chromate post-rinse treatment should be developed, which has equal or better corrosion resistance than does chromate post-rinse treatment. In this research, inorganic silicate with addition of Ca²⁺, Ba²⁺, Ni²⁺, Mg²⁺, has been extensively evaluated together with silane solution, γ -aminopropyltriethoxysilane ( γ -A.P.S., NH₂(CH₂)₃Si(OC₂H₅)₃), which was applied after the post-rinse treatment. The evaluation was carried out by the highly advanced surface analysis techniques such as SEM/EDX, AES, SIMS, and XRD and polarization measurements. / Master of Science
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Influencia dos parametros de processo na qualidade do revestimento de zinco/cobalto / Influence of depositon parameters on the quality of zinc/cobaltMachado, Carlos Henrique de Campos 13 August 2018 (has links)
Orientador: Rodnei Bertazzoli / Dissertação (mestrado) - Universidade Estadual de Campinas, Faculdade de Engenharia Mecanica / Made available in DSpace on 2018-08-13T22:40:42Z (GMT). No. of bitstreams: 1
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Previous issue date: 2009 / Resumo: o processo de deposição das ligas de zinco vem encontrando aplicações cada vez maiores na indústria de galvanoplastia, especificamente na produção de auto peças destinadas às empresas montadoras de veículos. Neste trabalho, o processo de deposição da liga Zn-Co foi estudado através da técnica de voltametria cíclica para kientificar as regiões de potenciais para a deposição dos constituintes da liga. A seguir, foram simuladas variações composicionais e operacionais do eletrólito para deposição da liga Zn-Co, normalmente observadas em linhas de produção. Adicionalmente, além das variações do eletrólito, foram estudadas amostras de peças (ferro fundido nodular como substrato) obtidas em condições adversas de processamento. O objeti,vo foi estudar a influência desses parâmetros na composição final do depósito, e na resistência à corrosão através de ensaios acelerados em câmara de névoa salina. O processo para deposição da líga Zn-Co apresentou boa estabilidade e', baixa sensibilidade às variações de concentração que podem ocorrer no cotidiano de uma linha de produção. Os ensaios em célula de Hull mostraram que variações deliberadas de 2 g.L-1 a 8 g.L-1 de Co (II) no banho produzem depósitos com 0,6 % a 1,6 % de Co na liga. Na faixa recomendada de trabalho de 4 g.L-1 a 6 g.L-1. obtém-se 0,9 % a 1,2 %. Os ensaios acelerados de corrosão em câmara de névoa salina mostraram que, mesmo nas condições mais improváveis de funcionamento, onde o teor de cobalto pode cair para 0,6 %, a camada resiste a mais de 500 horas de ensaio. Tempo de ensaio de 720 horas foi obtido quando [Zn(II)]=46 g.L-1 e [Co(II)]=4,6 g.L-1. ou seja, [Zn(II)]/[Co(II)]=10 / Abstract: Zinc alloy coatings have found large application in the metal finishing índustry, particularly for coatíng automotive parts. In thís work, the deposítíon of Zn-Co process was characterízed by cyclic voltammetry in order to identify the rangCe of deposition potential of the alloy and its constituents. Then, variations of deposition parameters and bath composition were símulated in order to study their influence on the coating properties. In addition, beside plating variation, samples produced under qnideal process condítion were studied. The plating bath presented good stability and low sensibility to variations usually observed in the industrial production. Hull-cell, experiments shown that, despite the deliberated changes in bath composítion, ,cobalt concentration in the alloy is always wíthín the range of 0,6 % to 1,6 %. Recommended values are from 0,9 % to 1,2 %. Salt spray tests shown that the Zn-Co coating lasted 500 h of test and, in the optimum deposition conditions, 720 h was obtained / Mestrado / Materiais e Processos de Fabricação / Mestre em Engenharia Mecânica
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Industrial waste minimisation in South Africa : a case study in the textile and metal finishing sectors.Reiner, Monika. January 2002 (has links)
Environmental legislation is becoming more stringent as people are realising the need for
conservation and a reduction of environmental degradation in order to facilitate sustainable
development. To ease legislative pressures, companies need to work together in symbiotic networks,
whereby co-operation between companies results in far more innovative practices than if the
companies acted individually. Success in an industrial network is largely dependent on cleaner
production, where industries seek to redirect from waste treatment to waste minimisation. Cleaner
production has already received international recognition and waste minimisation initiatives have
been used as a tool of cleaner production. Two polluting industrial sectors within South Africa, the
textile and metal finishing sectors, were chosen to investigate waste minimisation concepts. One
company from each sector was used as a case study. The dissertation followed company network
identification, potential to participate within an industrial symbiotic network, and waste
minimisation opportunities. Suppliers and buyers, up and down the product line were identified.
Relationships with these partners should be advanced such that environmental concerns are at the
forefront of any decision-making. In light of developing industrial networks and maintaining
symbiotic relationships, the company's potential was investigated by interviewing employees of
various ranks. Both companies were partially suited to participate within an industrial symbiotic
network and company-specific barriers were identified, such as ineffective internal communication.
The waste minimisation investigation followed a four-phase approach of planning and organisation;
pre-assessment; assessment; and feasibility study. In both the companies investigated, water savings
were identified as the waste minimisation focus area with potential for improvement. In total,
potential water savings of over R80 000 per annum were identified. In the textile company, the
weaving department and bleach house were further investigated. Cloth weaving errors were
attributed to machine stops, as each stop has the potential to result in a cloth fault. In the bleach
house the potential existed to reduce the number of rinse tanks. Although a modem and automated
process, the plating plant in the metal finishing company was identified as having potential waste
minimisation opportunities. Of particular interest was the reduction of solution carry over from the
plating tanks into subsequent tanks. Extended drip times were investigated. Additional waste
minimisation opportunities included repairing pipe leaks, replacing the degreasing solvent,
trichloroethylene, with a less harmful cleaning agent and establishing a symbiotic relationship with
the oil supplier, Castrol. Over and above the main waste minimisation opportunities highlighted,
other recommendations and potential savings were identified. Each case study emphasises that
simple waste minimisation initiatives, without expending capital, reduce demands on natural
resource, such as water, and benefit the company financially. Successful waste minimisation leads to
further cleaner production initiatives, which may then initiate better network interactions with the
further potential of promoting sustainable development. / Thesis (M.Sc.Eng.)-University of Natal, Durban, 2002.
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