Spelling suggestions: "subject:"entrace"" "subject:"biotrace""
1 |
Further exploration of C-11 HP target on PETtraceDick, D. W., Erdahl, C. E., Bender, B. R. 19 May 2015 (has links) (PDF)
Introduction
At WTTC 14 we presented data on the target yields of our GE PETtrace C-11 HP target in comparison to the target yields we had been getting on the MC17 prior to its decommissioning1. Discussion with other attendees alerted us to the fact that the target may be too “thin”, allowing the beam to spread out and interact with the walls, which could result in a lower target yield. Additionally, a GE service engineer indicated that we could be striking the top of the target with some of the beam, due both to target thinning and the “banana” effect from the magnetic fringe fields. Experiments were carried out to determine the potential magnitude of this effect and the efficacy of potential solutions.
Material and Methods
All experiments were performed on a GE PET-trace cyclotron. The first set of experiments was performed on the C-11 HP target in its natural mounting state (no aids). The change is gas pressure as a function of beam current was measured, from 5 to 70 microamps for three different gas fill pressures: 210, 230 and 250 PSI. The second set of experiments was performed after mechanically lifting the back end of the target with a box, changing the target angle from 23.9 degrees past horizontal to 25.2 degrees past horizontal. While this change in angle does not seem drastic, it did pick up all the slack in the target mount due the sagging of the target from its longer length than other GE targets. The change in gas pressure as a function of beam current was measured, from 5 to 80 microamps for four different gas fill pressures: 190, 210, 230 and 250 PSI. (Note that the box is a temporary solution and the target will sag over time without a more permanent solution for supporting the back end of the target.)
Results and Conclusion
The graphical results of pressure rise as a function of beam current are shown in FIGURE 1. Note that measurements were stopped when the pressure approached 470 PSI, based on advice from GE engineers. There is some flattening out for the 190-PSI data, even with the increase in angle as an attempt to counteract the banana effect (note that GE’s recommended fill pressure is 187 PSI). Increases in the fill pressure helped in keeping the target thick, but with the tradeoff that less beam can be put onto the target before reaching the maximum specified pressure. Final-ly, using a lifting mechanism to raise the back of the target also helped to prevent thinning, as seen in the r-squared values for the linear fit, shown in TABLE 1. The data presented indicate that a shorter target that can withstand higher pressures could be beneficial for the PETtrace cyclotron, allowing the beam to fully stop before striking the walls, be it through target thinning or the “banana” effect while still allowing the user to run high beam currents.
|
2 |
GE PETtrace RF power failures related to poor power qualityBender, B. R., Erdahl, C. E., Dick, D. W. 19 May 2015 (has links) (PDF)
Introduction
Anyone who has ever overseen the installation of a new cyclotron is aware of the importance of addressing the numerous vendor-supplied site specifications prior to its arrival. If the site is not adequately prepared, the facility may face project cost overruns, poor cyclotron performance and unintended maintenance costs. Once a facility has identified the space, providing sufficient power is the next step. Every cyclotron vendor will provide you with a set of power specifications, but meeting these specifications can be difficult, especially when the cyclotron is placed in an existing structure. The cyclotron is an interesting collection of power supplies providing power to sensitive electronic circuitry. It is not sufficient to just provide enough power; you must also provide quality power. It is hoped that our efforts to resolve our poor power quality problems will assist others as they replace aging cyclotrons in existing institutions whose power quality has degraded over the years.
The University of Iowa Hospitals and Clinics completed installation of a GE PETtrace 800 cyclotron in November 2011. Four months prior to installation, GE service personnel arrived to do a power assessment. The result was that we met their specifications, but with reservations. We could easily provide the quantity of power required, but the specification also states that GE recommends that primary power remain at 480 VAC ± 5%. GE service personnel attached a power quality analyzer to the cyclotron main power panel and determined that we did have some events of 7 to 8 % sag, but they were in-frequent, perhaps once or twice a week lasting 20 to 50 msec. Sags were confirmed to be the result of large non-linear loads elsewhere in the hospital. If these occurred during a run, they may shut down the cyclotron, specifically the RF power supply. Further investigation revealed the presence of harmonics on our power. Harmonics are the multiples of 60Hz power that are reflected back into your facility’s power grid from large motor drivers. Commercial air handler, water pump and fan motors often use variable frequency drives (VFDs) for proportional control to meet the changing facility demands. This pro-vides a significant on-going cost savings, but may play havoc with power quality throughout the institution.
Harmonic distortion is often quantified as a total harmonic distortion (THD) percentage. Though not specifically mentioned in the site-specifications, our experience here will show that it is important not to overlook harmonic distortion. Its effects can be varied, erratic and wide-spread throughout the cyclotron system. When asked, GE service referred us to IEEE standards for electrical systems and equipment which states that THD is recommended to be below 5 % for most applications, but below 3 % for sensitive settings including airports and hos-pitals1.
Mitigation of voltage sag and harmonic distortion is an expensive and complex topic. It is recommended that you consult with your cyclotron vendor to determine if there exists a field-tested solution. Additionally, you should consult a power systems specialist to do an audit of your building’s power system.
Material and Methods
Characterization of Power Quality: This was accomplished using a Hioki 3197 Power Quality Analyzer and a couple Dranetz PX-5 Power Xplorers. Each monitoring cycle logged data for about a week, which seemed to be about the limit for these units when logging both THD and surge/sag events down to the duration of a single 60Hz cycle. Analysis of the circuit diagrams and communication with GE engineers indicated that the main power contactors to the cyclotron RF system were dropping power to protect the system. The feedback for this shutoff is a detection signal from the front-end EHT (high-voltage generation) circuit that is set at a level to be representative of the 5% AC deviation specification.
RF Power System Contactors: Every time the contactors of the RF power distribution system are energized/de-energized, some arching occurs at the contact surfaces. This arching pits the contactor surfaces such that over time the contactor surfaces become irregular and potentially resistive. Since the RF protection circuit triggered by the EHT circuit is downstream from the contactors, it is not so hard to envision why the system becomes more sensitive over time2. Additionally, the harmonic distortion also exists on the AC voltage energizing the contactors. As a result, they may not actuate as smoothly (de-pendent of degree of harmonic distortion) and further hasten the normal rate of pitting of contactor surfaces.
Results and Conclusion
Within weeks of installation, we began to get RF power shutoffs. They were infrequent at first, but soon began to occur numerous times a week, then numerous times a day. At approximately 3 months post installation, it was often difficult to get through a standard 30 to 45 minute bombardment to make F-18 for our daily patient FDG doses. We limped along for over a year until the University was willing to invest in a solution to address our power problems.
Periodic Power Analyses: These analyses, per-formed over the next year, indicated that our power quality worsened in the winter and re-turned to functional levels in the summer. The instance of voltage sag remained approximately the same throughout the year (a few short sags per week), but the THD was down to 6 % in the summer and nearly 10% in the winter. This result, combined with RF shutdown tracking and lack of correlation between observed power sags and RF shutdowns, led us to the conclusion that our very high harmonic distortion combined with small power fluctuations (< 5 %) were the culprit.
Mitigation Planning: There are a number of power conditioning technologies, but imposing the need to remove both voltage sag as well as harmonic distortion, quickly narrows the field. What remains are the following options: 1) UPS line conditioner with batteries, 2) UPS line conditioner with flywheel or 3) motor-generator power isolator. Battery maintenance costs ruled out the UPS battery line conditioner. Of the remaining two, if you have the space, the motor-generator is the simplest and cheapest (favored by forward military hospital units). But for the space constrained user, like us, the UPS flywheel line conditioner became the preferred option.
Additionally, it was identified in a power audit that the THD was only 4% at the transformers connected directly to the local power utility company supply (upstream of load effect and harmonic distortion sources). This was to be expected as load effects and harmonic distortion are worse if your tie-in point to the building power grid is at the same level or downstream of their sources. Additionally, a test was performed during a hospital backup generator test, wherein the suspected primary offenders (large motors and VFDs) were diverted to backup. As a result, the THD measured at the cyclotron primary power panel dropped by 2.5 %.
Working with University electricians, an outside power consultant, GE engineering and University Hospital Radiology Engineering, a two phase plan was created.
Phase 1: With a repurposed utility transformer, the cyclotron and PET cameras got their own dedicated transformer connected to the main utility power feed. We also replaced the old contactors in the RF power distribution system. Since installation, the measured THD has remained at 4.5 to 5 % year round and the sag incidence and magnitude are slightly improved.
Phase 2: With a quote from GE for a flywheel UPS we should be able to fully condition the power entering our facility, removing the load effect voltage sags as well as the harmonic distortion.
One year of operation after Phase 1 implementation, it has been decided that Phase 1 was all that was required. We haven’t had a single new instance of RF shutdown since.
|
3 |
Further exploration of C-11 HP target on PETtraceDick, D. W., Erdahl, C. E., Bender, B. R. January 2015 (has links)
Introduction
At WTTC 14 we presented data on the target yields of our GE PETtrace C-11 HP target in comparison to the target yields we had been getting on the MC17 prior to its decommissioning1. Discussion with other attendees alerted us to the fact that the target may be too “thin”, allowing the beam to spread out and interact with the walls, which could result in a lower target yield. Additionally, a GE service engineer indicated that we could be striking the top of the target with some of the beam, due both to target thinning and the “banana” effect from the magnetic fringe fields. Experiments were carried out to determine the potential magnitude of this effect and the efficacy of potential solutions.
Material and Methods
All experiments were performed on a GE PET-trace cyclotron. The first set of experiments was performed on the C-11 HP target in its natural mounting state (no aids). The change is gas pressure as a function of beam current was measured, from 5 to 70 microamps for three different gas fill pressures: 210, 230 and 250 PSI. The second set of experiments was performed after mechanically lifting the back end of the target with a box, changing the target angle from 23.9 degrees past horizontal to 25.2 degrees past horizontal. While this change in angle does not seem drastic, it did pick up all the slack in the target mount due the sagging of the target from its longer length than other GE targets. The change in gas pressure as a function of beam current was measured, from 5 to 80 microamps for four different gas fill pressures: 190, 210, 230 and 250 PSI. (Note that the box is a temporary solution and the target will sag over time without a more permanent solution for supporting the back end of the target.)
Results and Conclusion
The graphical results of pressure rise as a function of beam current are shown in FIGURE 1. Note that measurements were stopped when the pressure approached 470 PSI, based on advice from GE engineers. There is some flattening out for the 190-PSI data, even with the increase in angle as an attempt to counteract the banana effect (note that GE’s recommended fill pressure is 187 PSI). Increases in the fill pressure helped in keeping the target thick, but with the tradeoff that less beam can be put onto the target before reaching the maximum specified pressure. Final-ly, using a lifting mechanism to raise the back of the target also helped to prevent thinning, as seen in the r-squared values for the linear fit, shown in TABLE 1. The data presented indicate that a shorter target that can withstand higher pressures could be beneficial for the PETtrace cyclotron, allowing the beam to fully stop before striking the walls, be it through target thinning or the “banana” effect while still allowing the user to run high beam currents.
|
4 |
GE PETtrace RF power failures related to poor power qualityBender, B. R., Erdahl, C. E., Dick, D. W. January 2015 (has links)
Introduction
Anyone who has ever overseen the installation of a new cyclotron is aware of the importance of addressing the numerous vendor-supplied site specifications prior to its arrival. If the site is not adequately prepared, the facility may face project cost overruns, poor cyclotron performance and unintended maintenance costs. Once a facility has identified the space, providing sufficient power is the next step. Every cyclotron vendor will provide you with a set of power specifications, but meeting these specifications can be difficult, especially when the cyclotron is placed in an existing structure. The cyclotron is an interesting collection of power supplies providing power to sensitive electronic circuitry. It is not sufficient to just provide enough power; you must also provide quality power. It is hoped that our efforts to resolve our poor power quality problems will assist others as they replace aging cyclotrons in existing institutions whose power quality has degraded over the years.
The University of Iowa Hospitals and Clinics completed installation of a GE PETtrace 800 cyclotron in November 2011. Four months prior to installation, GE service personnel arrived to do a power assessment. The result was that we met their specifications, but with reservations. We could easily provide the quantity of power required, but the specification also states that GE recommends that primary power remain at 480 VAC ± 5%. GE service personnel attached a power quality analyzer to the cyclotron main power panel and determined that we did have some events of 7 to 8 % sag, but they were in-frequent, perhaps once or twice a week lasting 20 to 50 msec. Sags were confirmed to be the result of large non-linear loads elsewhere in the hospital. If these occurred during a run, they may shut down the cyclotron, specifically the RF power supply. Further investigation revealed the presence of harmonics on our power. Harmonics are the multiples of 60Hz power that are reflected back into your facility’s power grid from large motor drivers. Commercial air handler, water pump and fan motors often use variable frequency drives (VFDs) for proportional control to meet the changing facility demands. This pro-vides a significant on-going cost savings, but may play havoc with power quality throughout the institution.
Harmonic distortion is often quantified as a total harmonic distortion (THD) percentage. Though not specifically mentioned in the site-specifications, our experience here will show that it is important not to overlook harmonic distortion. Its effects can be varied, erratic and wide-spread throughout the cyclotron system. When asked, GE service referred us to IEEE standards for electrical systems and equipment which states that THD is recommended to be below 5 % for most applications, but below 3 % for sensitive settings including airports and hos-pitals1.
Mitigation of voltage sag and harmonic distortion is an expensive and complex topic. It is recommended that you consult with your cyclotron vendor to determine if there exists a field-tested solution. Additionally, you should consult a power systems specialist to do an audit of your building’s power system.
Material and Methods
Characterization of Power Quality: This was accomplished using a Hioki 3197 Power Quality Analyzer and a couple Dranetz PX-5 Power Xplorers. Each monitoring cycle logged data for about a week, which seemed to be about the limit for these units when logging both THD and surge/sag events down to the duration of a single 60Hz cycle. Analysis of the circuit diagrams and communication with GE engineers indicated that the main power contactors to the cyclotron RF system were dropping power to protect the system. The feedback for this shutoff is a detection signal from the front-end EHT (high-voltage generation) circuit that is set at a level to be representative of the 5% AC deviation specification.
RF Power System Contactors: Every time the contactors of the RF power distribution system are energized/de-energized, some arching occurs at the contact surfaces. This arching pits the contactor surfaces such that over time the contactor surfaces become irregular and potentially resistive. Since the RF protection circuit triggered by the EHT circuit is downstream from the contactors, it is not so hard to envision why the system becomes more sensitive over time2. Additionally, the harmonic distortion also exists on the AC voltage energizing the contactors. As a result, they may not actuate as smoothly (de-pendent of degree of harmonic distortion) and further hasten the normal rate of pitting of contactor surfaces.
Results and Conclusion
Within weeks of installation, we began to get RF power shutoffs. They were infrequent at first, but soon began to occur numerous times a week, then numerous times a day. At approximately 3 months post installation, it was often difficult to get through a standard 30 to 45 minute bombardment to make F-18 for our daily patient FDG doses. We limped along for over a year until the University was willing to invest in a solution to address our power problems.
Periodic Power Analyses: These analyses, per-formed over the next year, indicated that our power quality worsened in the winter and re-turned to functional levels in the summer. The instance of voltage sag remained approximately the same throughout the year (a few short sags per week), but the THD was down to 6 % in the summer and nearly 10% in the winter. This result, combined with RF shutdown tracking and lack of correlation between observed power sags and RF shutdowns, led us to the conclusion that our very high harmonic distortion combined with small power fluctuations (< 5 %) were the culprit.
Mitigation Planning: There are a number of power conditioning technologies, but imposing the need to remove both voltage sag as well as harmonic distortion, quickly narrows the field. What remains are the following options: 1) UPS line conditioner with batteries, 2) UPS line conditioner with flywheel or 3) motor-generator power isolator. Battery maintenance costs ruled out the UPS battery line conditioner. Of the remaining two, if you have the space, the motor-generator is the simplest and cheapest (favored by forward military hospital units). But for the space constrained user, like us, the UPS flywheel line conditioner became the preferred option.
Additionally, it was identified in a power audit that the THD was only 4% at the transformers connected directly to the local power utility company supply (upstream of load effect and harmonic distortion sources). This was to be expected as load effects and harmonic distortion are worse if your tie-in point to the building power grid is at the same level or downstream of their sources. Additionally, a test was performed during a hospital backup generator test, wherein the suspected primary offenders (large motors and VFDs) were diverted to backup. As a result, the THD measured at the cyclotron primary power panel dropped by 2.5 %.
Working with University electricians, an outside power consultant, GE engineering and University Hospital Radiology Engineering, a two phase plan was created.
Phase 1: With a repurposed utility transformer, the cyclotron and PET cameras got their own dedicated transformer connected to the main utility power feed. We also replaced the old contactors in the RF power distribution system. Since installation, the measured THD has remained at 4.5 to 5 % year round and the sag incidence and magnitude are slightly improved.
Phase 2: With a quote from GE for a flywheel UPS we should be able to fully condition the power entering our facility, removing the load effect voltage sags as well as the harmonic distortion.
One year of operation after Phase 1 implementation, it has been decided that Phase 1 was all that was required. We haven’t had a single new instance of RF shutdown since.
|
Page generated in 0.0413 seconds