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INVESTIGATION OF THE EFFECTIVENESS OF AN INTEGRATED FLOODED-BED DUST SCRUBBER ON A LONGWALL SHEARER THROUGH LABORATORY TESTING AND CFD SIMULATIONArya, Sampurna N. 01 January 2018 (has links)
Dust generation at an underground coal mine working face continues to be a health and safety issue. Prolonged exposure to high concentrations of airborne respirable dust can cause a debilitating and often fatal respiratory disease called Black Lung. In addition, the deposition of float dust in mine return airways poses a serious safety hazard if not sufficiently diluted with inert rock dust. A localized methane explosion can transition into a self-propagating dust explosion. Since dust is a byproduct of various mining activities, such as cutting and loading, crushing, and transportation, the dust-related issues cannot be totally eliminated. However, the adverse health effects and safety concerns can be minimized if a significant amount of the generated dust is removed from the ventilation air by a mechanical device, such as a dust scrubber.
Over the last three decades, flooded-bed dust scrubbers integrated into continuous miners have been successfully applied for capturing and removing airborne dust generated at the working face. According to the National Institute for Occupational Safety and Health (NIOSH), a flooded-bed scrubber can achieve more than 90% capture and cleaning efficiencies under optimum conditions. Although flooded-bed scrubbers have proven useful in the vast majority of cases, they have not yet been successfully applied to a longwall face.
In the United States, numerous attempts have been made to reduce dust concentration at a longwall face through the application of a scrubber; but, none were successfully implemented. Encouraged by the successful use of a flooded-bed scrubber system at continuous miner faces, this research revisits the flooded-bed scrubber concept for a longwall shearer. For this investigation, a full-scale physical model of a Joy 7LS longwall shearer, modified with an integrated flooded-bed dust scrubber, was designed and fabricated at the University of Kentucky. The scope of work for this research was limited to capturing and cleaning dust generated near the shearer headgate drum only. The mock-up was transported to, and assembled in, the full-scale longwall dust gallery at the NIOSH Pittsburgh Research Laboratory (PRL).
Tests were conducted to examine: (1) the effect of the scrubber on headgate-drum dust reduction and (2) the combined effect of the scrubber and splitter sprays on headgate drum dust reduction. Analysis of test results for the scrubber-alone condition indicates a significant dust reduction of up to 57% in the return airway and 85% in the test gallery walkway, whereas the combination of scrubber and splitter-arm sprays shows dust reduction of up to 61% and 96% in the return and walkway, respectively. These results indicate that a flooded-bed scrubber integrated into a longwall shearer can be used as a viable technique to reduce a large portion of airborne dust at a longwall face.
Subsequently, a Computational Fluid Dynamics (CFD) model of the longwall gallery and shearer was developed and validated using the results of the experimental study. The CFD simulation results are in good agreement with the experimental results with a maximum of 9.7% variation. This validated CFD model can be used in future research to predict the effects of modifications to the scrubber system, including modifications to the scrubber inlet, to optimize the scrubber design, and to evaluate the effectiveness of adding a tailgate drum dust scrubber.
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Automated Multidisciplinary Optimizations of Conceptual Rocket FairingsSmart, Ronald S. 13 July 2011 (has links) (PDF)
The purpose of this research is to develop and architect a preliminary multidisciplinary design optimization (MDO) tool that creates multiple types of generalized rocket fairing models. These models are sized relative to input geometric models and are analyzed and optimized, taking into account the primary objectives, namely the structural, thermal, and aerodynamic aspects of standard rocket flights. A variety of standard nose cone shapes is used as optimization proof of concept examples, being sized and compared to determine optimal choices based on the input specifications, such as the rocket body geometry and the specified trajectory paths. Any input models can be optimized to their respective best nose cone style or optimized to each of the cone styles individually, depending on the desired constraints. Two proof of concept example rocket model studies are included with varying sizes and speeds. Both have been optimized using the processes described to provide delineative instances into how results are improved and time saved. This is done by optimizing shape and thickness of the fairings while ascertaining if the remaining length downstream on the designated rocket model remains within specified stress and temperature ranges. The first optimized example exhibits a region of high stress downstream on the rocket body model that champions how these tools can be used to catch weaknesses and improve the overall integrity of a rocket design. The second example demonstrates how more established rocket designs can decrease their weight and drag through optimization of the fairing design.
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