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  • About
  • The Global ETD Search service is a free service for researchers to find electronic theses and dissertations. This service is provided by the Networked Digital Library of Theses and Dissertations.
    Our metadata is collected from universities around the world. If you manage a university/consortium/country archive and want to be added, details can be found on the NDLTD website.
1

High-frequency Quasi-square-wave Flyback Regulator

Zhang, Zhemin 02 December 2016 (has links)
Motivated by the recent commercialization of gallium-nitride (GaN) switches, an effort was initiated to determine whether it was feasible to switch the flyback converter at 5 MHz in order to improve the power density of this versatile isolated topology. Soft switching techniques have to be utilized to eliminate the switching loss to maintain high efficiency at multi-megahertz. Compared to the traditional modeling of zero-voltage-switching quasi-square-wave converters, a numerical methodology of parameters design is proposed based on the steady-state model of zero-voltage switching quasi-square-wave flyback converter. The magnetizing inductance is selected to guarantee zero-voltage switching for the entire input and load range with the trade-off design for conduction loss and turn-off loss. A design methodology is introduced to select a minimum core volume for an inductor or coupled inductors experiencing appreciable core loss. The geometric constant Kgac = MLT/(Ac2WA) is shown to be a power function of the core volume Ve, where Ac is the effective core area, WA is the area of the winding window, and MLT is the mean length per turn for commercial toroidal, ER, and PQ cores, permitting the total loss to be expressed as a direct function of the core volume. The inductor is designed to meet specific loss or thermal constraints. An iterative procedure is described in which two- or three-dimensional proximity effects are first neglected and then subsequently incorporated via finite-element simulation. Interleaved and non-interleaved planar PCB winding structures were also evaluated to minimize leakage inductance, self-capacitance and winding loss. The analysis on the trade-off between magnetic size, frequency, loss and temperature indicated the potential for a higher density flyback converter. A small-signal equivalent circuit of QSW converter was proposed to design the control loop and to understand the small-signal behavior. By adding a simple damping resistor on the traditional small-signal CCM model, it can predict the pole splitting phenomenon observed in QSW converter. With the analytical expressions of the transfer functions of QSW converters, the impact of key parameters including magnetizing inductance, dead time, input voltage and output power on the small-signal behavior can be analyzed. The closed-loop bandwidth can be pushed much higher with this modified model, and the transient performance is significantly improved. With the traditional fix dead-time control, a large amount of loss during dead time occurred, especially for the eGaN FETs with high reverse voltage drop. An adaptive dead time control scheme was implemented with simple combinational logic circuitries to adjust the turn on time of the power switches. A variable deadtime control was proposed to further improve the performance of adaptive dead-time control with simplified sensing circuit, and the extra conduction loss caused by propagation delay in adaptive dead-time control can be minimized at multi-megahertz frequency. / Ph. D. / With the fast development of telecom, computer and network systems, high efficient and small volume power supplies are highly desired. A typical method for achieving high power density involves increasing the frequency and implement soft-switching techniques to minimize loss. Thanks to the recent commercialization of the advanced semiconductor gallium-nitride (GaN) switches, it is feasible to design high density power supplies and cost effective power system. Several challenges including optimization of power converter, high frequency magnetics and implementation of control architecture have been addressed in this dissertation which helps to realize this compact power system. With the implementation of proposed circuit model and seminumerical design procedures for magnetics, a 30W high-frequency isolated DC/DC converter with planar inductor is fabricated to verify the theoretical analysis, which also demonstrates much improved performances.
2

Theoretical Analysis and Design for the Series-Resonator Buck Converter

Tu, Cong 03 February 2023 (has links)
High step-down dc/dc converters are widely adopted in a variety of areas such as industrial, automotive, and telecommunication. The 48 V power delivery system becomes increasingly popular for powering high-current and low-voltage chips. The Series-Capacitor Buck (SCB) converter doubles the duty ratio and equalizes the current between the two phases. Hard switching has hindered efforts to reduce volume via increased switching frequency, although a monolithically integrated SCB converter has boosted current density. A Series-Resonator Buck (SRB) converter is realized by adding a resonant tank in series with the series capacitor Cs. All switches turn on at zero-voltage (ZVOn), and the low-side switches turn off at zero-current (ZCOff). The design of the SRB converter includes characterizing the design variables' impacts on the converter performances and designing low-loss resonant components as the series resonator. The Series-Resonator Buck converter belongs to the class of quasi-resonant converters. Its resonant frequency is higher than the switching frequency, and its waveforms are quasi-sinusoidal. This work develops a steady-state model of the SRB converter to calculate voltage gain, component peak voltages, and resonant inductor peak current. Each switching cycle is modeled based on the concept of generalized state-space averaging. The soft-switching condition of the high-side switches is derived. The ZVS condition depends on the normalized control variable and the load condition. The gain equation models the load-dependent characteristic and the peak gain boundary. The theoretical peak voltage gain of the SRB converter is smaller than the maximum gain of the SCB converter. A smaller normalized load condition results in a larger peak voltage gain of the SRB converter. The large-signal model of the SRB converter characterizes the low-frequency behavior of the low-pass filters with the series capacitor and the high-frequency behavior of the resonant elements. A design recommendation of t_off f_r<0.5 is suggested to avoid the oscillation between the series capacitor Cs and the output inductors Lo. In other words, the off-duration of the low-side switches is less than half of 1/fr, and therefore the negative damping effect from the parallel resonant tank to the vCs response is reduced. The transfer functions of the SRB converter are presented and compared with those of the SCB converter. The series resonator brings in an extra damping effect to the response of output capacitor voltage. The understanding of the analytical relationships among the resonant tank energy, voltage gain, and component stresses was utilized to guide the converter design of the converter's parameters. A normalized load condition at √2 minimizes the stresses of the series resonator by balancing the peak energy in the resonant elements Lr and Cr. The f_s variation with voltage gain M is less than 10%. The non-resonant components C_s, L_oa, and L_ob are designed according to the specified switching ripples. The ac winding loss complicates the winding design of a resonant inductor. This work replaces the rectangular window with a rhombic window to reduce the eddy current loss caused by the fringing effect. The window ratio k_y is added as a design variable. The impacts of the design variables on the inductance, core loss, and winding loss are discussed. The air-gap length l_g is designed to control the inductance. A larger k_y design results in a short inductor length l_c and a smaller winding loss. The disadvantages include a smaller energy density design and a larger core loss due to the smaller cross-sectional area. In the design example presented in the thesis, the presence of the rhombic shape increases the gap-to-winding distance by two times, and also reduces the y-component of the magnetic field by a factor of two. The total inductor loss is reduced by 56% compared to a conventional design with a rectangular winding window while keeping the same inductance and the same inductor volume. This dissertation implements a resonator, replacing the series capacitor, in an SCB converter. The resultant SRB converter shows a 30% reduction in loss and a 50% increase in power density. The root cause of the divergence issue is identified by modeling the negative damping effect caused by resonant elements. The presented transient design guideline clears the barriers to closed-loop regulation and commercialization of the SRB converter. This work also reshapes winding windows from rectangle to rhombus which is a low-cost change that reduces magnetic loss by half. The theoretical analysis and design procedures are demonstrated in a 200 W prototype with 7% peak efficiency increase compared to the commonly used 30 W commercial SCB product. / Doctor of Philosophy / High step-down dc/dc converters are widely adopted in a variety of areas such as industrial, automotive, and telecommunication areas. The 48 V power delivery system becomes increasingly popular for powering high-current and low-voltage chips. The Series-Capacitor Buck (SCB) converter doubles the duty ratio and equalizes the current between the two phases. Hard switching has hindered efforts to reduce volume via increased switching frequency although a monolithically integrated SCB converter has boosted current density. A Series-Resonator Buck (SRB) converter is realized by adding a resonant tank in series with the series capacitor Cs. All switches turn on at zero-voltage (ZVOn), and the low-side switches turn off at zero-current (ZCOff). The challenges to designing the SRB converter include characterizing the design variables' impacts on the converter performances and designing low-loss resonant components as the series resonator. The resultant SRB converter shows a 30% reduction in loss and a 50% increase in power density. The root cause of the divergence issue is identified by modeling the negative damping effect caused by the resonant elements. The presented transient design guideline clears the barriers of closed-loop regulation and commercialization of the SRB converter. This work also reshapes winding windows from rectangle to rhombus, which is a low-cost change that reduces magnetic loss by half. The theoretical analysis and design procedures are demonstrated in a 200 W prototype with 7% peak efficiency increase compared to the commonly used 30 W commercial SCB product.

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