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Characterization of High Momentum Flux Combustion Powered Fluidic Actuators for High Speed Flow ControlWarta, Brett James 15 November 2007 (has links)
The performance of a high-power small-scale combustion-based fluidic actuator for high-speed flow control applications is characterized with specific focus on comparisons between premixed and nonpremixed operating modes for the device. Momentary (pulsed) actuation jets are produced by the ignition of a mixture of gaseous fuel and oxidizer within a small (cubic centimeter scale) combustion chamber. The combustion process yields a high pressure burst (1 to 3 ms in duration in the typical configurations) and the ejection of a high-speed exhaust jet. The actuation frequency can be continuously varied by independently controlling the flow rate of the fuel/oxidizer and the spark ignition frequency up to a maximum determined by the operating characteristics of the actuator. The actuator performance is characterized by both its peak thrust and net total impulse, with increases in peak jet momentum often two to three orders of magnitude above the baseline steady jet. Results for operation of the device in both premixed and nonpremixed modes are presented and analyzed, with nonpremixed operation typically yielding higher pressures and greater frequency ranges in the present configurations.
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Wind Tunnel and Flight Testing of Active Flow Control on a UAVBabbar, Yogesh 2010 May 1900 (has links)
Active flow control has been extensively explored in wind tunnel studies but successful in-flight implementation of an active flow control technology still remains a challenge. This thesis presents implementation of active flow control technology onboard a 33% scale Extra 330S ARF aircraft, wind tunnel studies and flight testing of fluidic actuators. The design and construction of the pulsed blowing system for stall suppression (LE actuator) and continuous blowing system for roll control (TE actuator) and pitch control have been presented. Full scale wind tunnel testing in 7̕ X 10 Oran W. Nicks low speed wind tunnel shows that the TE actuators are about 50% effective as the conventional ailerons. The LE actuator is found to be capable of suppressing stall from 12° to about 22°. Comparison of characteristics of Active elevator and conventional elevator in 3' X 4' low speed wind tunnel show that, the active elevator is as effective as of conventional elevator deflected at 5°. Flight tests show that TE actuators are able to control the aircraft in flight in banked turns. The measured roll rates in-flight support the wind tunnel test findings.
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Techniques to inject pulsating momentumKranenbarg, Jelle January 2020 (has links)
Hydro power plants are an essential part of the infrastructure in Sweden as they stand for a large amount of the produced electricity and are used to regulate supply and demand on the electricity grid. Other renewable energy sources, such as wind and solar power, have become more popular as they contribute to a fossil free society. However, wind and solar power are intermittent energy sources causing the demand for regulating power on the grid to increase. Hydro power turbines are designed to operate at a certain design point with a specific flow rate. The plants are operated away from the design point when used to regulate the supply and demand of electricity. This can cause a specific flow phenomenon to arise in the draft tube at part load conditions called a Rotating Vortex Rope (RVR) which causes dangerous pressure fluctuation able to damage blades and bearings. A solution to mitigate a RVR is to inject pulsating momentum into the draft tube by using an actuator operating at a certain frequency. A literature study was conducted and three techniques were numerically simulated using ANSYS Workbench 19.0 R3; a fluidic oscillator, a piston actuator and a synthetic jet actuator. A dynamic mesh was used to simulate the movement of the piston actuator and diaphragm of the synthetic actuator whilst the mesh of the fluidic oscillator was stationary. The relative errors of the three numerical models were all below 3 %. All devices showed promising results and could potentially be used to mitigate a RVR because they all have the ability to produce high energy jets. The fluidic oscillator had an external supply of water, whereas the other two did not, which means that it could inject the largest mass flow. The piston actuator required a driving motor to move the piston. The diaphragm of the synthetic jet actuator was moved by a Piezoelectric element. Advantages of the fluidic oscillator are that it has no moving parts, in contrary to the two other devices, it can directly be connected to the penstock or draft tube to obtain the required water supply and it is easy to install. It will most likely also be smaller compared to the other two for the same mass flow rate. It does however not generate a pulsating jet, but rather an oscillating jet. The other two devices generate pulsating jets, but have problems with low pressure areas during the intake stroke which can cause cavitation problems. These areas cause the formation of vortex rings close to the outlet. Simulations showed that a coned piston together with a coned cylinder outlet could decrease losses by almost 16 % compared to a normal piston and cylinder. It also decreased the risk for cavitation and the required force to move the piston. Otherwise, a shorter stroke length for a constant cylinder diameter or a longer stroke length for a constant volume displacement also decreased the risk for cavitation and required force. The gasket between the piston and cylinder is a potential risk for leakage. A solution to avoid critical low pressure areas is to install an auxiliary fluid inlet or valve which opens at a certain pressure for the piston actuator as well as the synthetic jet actuator. This will also allow larger mass flow rates and a higher injected momentum. Both devices are more complicated to install and require likely more maintenance compared to the fluidic oscillator. However, there exist many possible design options for the piston actuator. The design of the synthetic jet is more limited because of the diaphragm. The amplitude of the diaphragm also has a direct effect on the pressure levels. The losses increased proportional to the mass flow to the power of three which suggests that it is better to install many small actuators instead of a few large ones.
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